Philosophy 102:
The Tao of Rigging - Part II
In Part I of this article, we covered what went into rigging Toy Boat 2 prior to launch. Now we'll fast-forward four years, and discuss where we are now and how we got there...SLAGIATT stands for "Seemed Like A Good Idea At The Time". In this sections we cover things that we did in TB2 for first launch that turned out to be mistakes, and how we fixed them. Overall, there weren't that many...
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What we hadn't counted on was the low power of the radio speakers. In this position, it was virtually impossible to hear the radio clearly, even on full volume, if we were standing up behind the wheel.
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![]() We relocated the radio (which is JIS-7 rated) externally to the side of the console. We got this idea from Mike Lewis, owner of Western Eagle Boats, who has a similar mount on his personal WE18 skiff. We covered the hole in the dashboard with a binocular holder tray.
On our first attempt at mounting the radio externally, we ran the wiring through a cable clam into the console. The idea was to protect the connectors on the power and NMEA cables by placing them inside the console. This later turned out to be too tight a fit (the radio-side cables were too short), so we simply ran the cables under the bottom edge of the console. A drip loop protects the console from water running down the cable. |
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VHF Radio Antenna We do a lot of fly fishing, so we originally got a 3' whip antenna and put it on a rachet mount on the console rail. The idea was to allow us to swing the antenna straight down to provide clearance for casting. |
This turned out to be a big mistake. Transmit range was very short, as could be predicted. |
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Standard Horizon FF41 Fuel Flow Meter
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Performance was erratic at best, sometimes good, sometimes waaaay off. |
We tried a number of things (see the Project Boat Scorecard), ultimately, it turned out that locating the transducer vertically inside the transom, above the filter completely fixed the problem. Now the FF41 is accurate to within 3% or less. This would not have been possible, had we not repowered. By repowering, we were able to clear out a mess of engine harness adapter wiring that was in the transom for the old motor, freeing up space for the fuel flow meter transducer. |
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The stock rod holder on the back of the Cannon Unitroll HP was too small to accomodate any of our ocean-going rods. The plastic mount point also looked too weak to retain a 30lb class trolling rod on the strike. Because the downrigger mount was in one of the gunnel rod-holders, there was no other place to set the rod if we were trolling another rod on that side. |
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Unfortunately, this also made it very difficult to turn the switch on and off. Opening the tilt console to access the switch was difficult at best.
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We were going to spin the single switch around and have it face outward, but decided to go to three waterproof mini-switches as per a West Marine Advisor. We also turned the trolling motor circuit breaker outboard as well. |
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We added a permanent downrigger mount on the starboard stern
corner, and removed the rodholder from the downrigger. The downrigger rod now
goes into the closest gunnel rod holder (visible behind the cleat).
